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  • Replication of room-temperature superconductor claims fails to show superconductivity

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    • 297 views
    • 3 minutes

    A team of physicists at Nanjing University, attempting to replicate the superconductivity results from an experiment conducted by a team at the University of Rochester, produced the desired material but also found that it was not superconductive. In their study, reported in the journal Nature, the group replicated the work by the prior team and tested the resulting material.

     

    In 2020, a team of engineers and physicists at the University of Rochester in New York, led by mechanical engineer Ranga Dias, published a paper in the journal Nature claiming to have created a compound that, when exposed to extreme pressure, became a superconductor at room temperature. Soon thereafter, Nature retracted the paper due to the use of undocumented data by the research team.

     

    More recently, the same team published another paper in Nature claiming to have created a different material that became superconductive at room temperature—at much lower pressure than the material described in their first paper. In this new effort, the team in China duplicated the work, hoping to find the same results.

     

    The work involved following the same steps taken by the team at the University of Rochester (UoR), doping a lutetium-hydrogen chemical with nitrogen. The idea behind the effort is that hydrogen-rich chemicals can, under the right conditions, incite the formation of Cooper pairs of electrons, which have been associated with superconductivity.

     

    The team in China found that the process did lead to the formation of a compound that at first glance appeared to be identical to that created by the team at UoR. A closer look using an X-ray machine showed its structure, a hydrogen-lutetium-nitrogen compound, that looked nearly identical to the UoR compound. And testing with Ramen spectroscopy showed it had the same vibrational frequencies. The Chinese team even found the same color changes reported by the UoR team as the material was subjected to high pressure.

     

    Unfortunately, things did not look the same when the material was tested for superconductivity. The team in China was not able to detect any transition changes, even when they tested it at super-cold temperatures.

     

    The Chinese team is not rejecting the results obtained by the team at UoR—instead, they suggest it is possible that the nitrogen dopant present in their material was of insufficient quantity to produce the desired effect. They also note that in their sample, the dopant was unevenly distributed. They suggest further testing is needed to verify the results obtained by the group at UoR.

     

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